Restoring an Austin Seven Special
An Austin Seven restoration/renovation project can take months, years or, with
gradual loss of enthusiasm and interest, it may never be finished.
It will be left
to lanquish or sold to another enthusiast who might try to finish the
project. Here presented, is the tale of renovating a
Special for the second time - a true labour of love.
Pt 1 - Scouse special
I first acquired AMC 250, a 1933 Austin Seven Special, in 1967
while still at school. My parents were on holiday when I saw it
for sale in 'Exchange and Mart' near London for £45. It wasn’t a
runner, and the first attempts to make it go were in Cambridge with my
mates Donald and Malcolm pushing. The spark plugs were connected in the
logical order 1,2,3,4 and sometimes the wheels would spin backwards as
we got a partial fire. It took 3-years to get the car on the road and
legal, by which time it was with me at University in Liverpool. The
final stages of renovation were done in my ground-floor bedroom, having
passed the car in through the big bay window to work on it in the dry.

Sefton Park c 1970
Once roadworthy, and shortly after passing my driving test, I can
remember speeding down Liverpool’s Otterspool Promenade and drifting round the roundabouts. The car was a
competent attempt at a special, without being too radical. The standard
1933 A7 chassis was shortened and lowered, and the body was aluminium on
an ash frame with steel cycle wings and the spare, spoked wheel carried
on the back. The engine had a Dante high compression (6:1) head and twin
SU carburettors. Brakes were Morris Minor hydraulics. It was fun to
drive, and I used it for trips to Wales and Scotland.
After University
I started travelling the world, so sold the car to a University friend, Ern, who was a student doctor, in 1972. He and his wife Anne both
became GPs in Yorkshire and took the car there. Ern put the car in a
shed, which collapsed, crushing it amidships. I saw it there in 1999,
still trapped. Ern eventually freed the car and started to dismantle it
for restoration. Unfortunately, the engine and some ancillaries
(radiator, starter motor…) were stolen and enthusiasm was lost.
When Ern decided to get rid of the car in order to carry out
modifications to the house and outbuildings, he rang me around Christmas
2018 to ask if I wanted it back.

As it arrived at Veryan, Feb 2019
I jumped at the chance, so Ern and
Anne brought it down in a box trailer in
February 2019. They would only accept the cost of hiring the trailer
(£120) for the car despite my best effort at paying them more.
Being in the middle of the full restoration of a 1975 BMW R90S
motorcycle I had to complete that before I could start on the Austin.
Joining the Cornwall Austin Seven Club has been a good
move and something of a revelation. I have owned a 1931 Austin Ulster
replica since 1999, and campaigned it successfully in the Classic Monte
Carlo Rally of 2000, but hadn’t been aware of the Club. Meeting Andrew
Jarmin, and being shown round his collection and workshops, demonstrated
what I had been missing. The Club gives me added confidence in taking on
the restoration, together with local friends who have astonishing skills
that will be relevant and called upon.
Pt 2 - On time and off budget

It is easy to be overwhelmed and I knew I was in for a
major project so the first thing was to get it into a dry workshop and sort
the bits I had into boxes. It was a little depressing as quite a bit was missing. Luckily I had a “spare” engine, but this was also minus the fan
assembly, starter motor, clutch, water inlet, oil filler tube, oil
pressure union, dipstick etc.
Into the workshop
First to be
fettled was the dynamo. A quick whizz on Andrew’s rig showed that it
worked. Its polarity was changed to negative earth and the output set,
using the third brush, at 10 amps. The 4-speed gearbox
with synchromesh on third and fourth took a bit longer, but over the
course of an enjoyable day in which I learned a lot at Andrew’s elbow we
installed new bearings, balls and springs.
The distributor shaft was
seized, so I worked it and drenched it in WD40 until it started moving. I then ordered new rotor arm, condenser and points and assumed that the
job was done. Not so. I took the base plate off and was met with a red
mess of corrosion in which the advance weights were well stuck. Again I
worked manfully to free these and their springs. One spring was broken,
but eventually the weights started to move and even return feebly. However, I decided that the wear in the shaft/bushes was too much and
despatched the whole unit to The Distributor Doctor for a complete
rebuild. looked into electronic ignition but couldn’t find anyone who
makes good quality units for the Seven. A bonus was that Martin
Jay at DD
also runs trials Sevens and offered me a windscreen.

My idea
was to get the Special on the road, but not to attempt to make it
concours. However, whatever I touched seemed to need work, so eventually
I decided to take the body off in order to fettle the chassis, shock
absorbers, springs, steering and brakes. The aluminium on ash body
was built by Super Accessories in Kent, probably in the early 1960s, and
comprises a whole jigsaw of panels, none being particularly complicated. Good thing as I’m going to have to make quite a few of them as they were
buckled and torn by the shed collapsing on them.
That is for later. For now I decided to
concentrate on building up a rolling chassis. The rear and front springs
were pretty good and only needed new U-bolts on the rear springs. The
rear shock absorbers were a very unmatched pair, so I bought new ones. I
also bought a good second-hand radius arm from Holmesdale Sevens as one
was original and one a replacement at some time in the car’s history. I
have fitted a new double front shock absorber purchased with new links
and bushes from the Austin Seven Workshop to improve handling. I removed
the steering column and box and have yet to assess the whole steering
system.

Next to come off were the prop shaft and torque tube. What I thought was
play in the torque tube turned out to be a crack around the outer tube. I rang Andrew to ask if he advised welding. No, he said, bring it round
and I’ll sort it. And true to his word he and his Sorcerer’s Apprentice
(me) replaced the outer tube with one he had in his store. Meanwhile I’m
thinking that I’d better start to source the missing bits from the
engine. I have the Supaloy high compression head, twin SUs and Dante
bunch of bananas manifold that were on the car when I had it between
1967 and 1972. But I didn’t have a starter motor. Much interneting later
I persuaded Tony Leslie of Holmesdale Sevens to make me a suitable
starter from bits he had. Bless him he did it and then I discovered that
the mix of 1930 engine I have, mated to the larger 1933 4-speed gearbox,
is incompatible with a standard starter without quite a bit of
re-engineering. Fortunately Andrew had a solution and the early
“bacon-slicer” starter fits with only the need to shave a bit off the
housing.

I
mentioned earlier that I did not have a clutch. Indeed the only clutch bit I had
was the (good) clutch lining on the flywheel. Andrew fished a pressure
plate complete with worn starter ring gear from somewhere but even he
didn’t know how I was going to renew the ring. I consulted and
researched the interweb thing. Tony Leslie came up with the clutch bits
I was short of, and recommended that I send them all, with a new starter
ring to Paul Bonewell in Sussex. He is a whizz engineer who reprofiles
camshafts for racing Austin Sevens and the like. He machined off the old
ring and shrank on the new one as well as assembling the clutch so that
I can just slot it in. Brilliant.

And that is about as far as I’ve got so far apart from painting the
chassis and cleaning loads of parts for the Big Build. I’m still not
ready to start that. I need to check the engine over carefully as it has
been idle for 10 years; I need to get brake parts (Morris Minor 7”
hydraulics), and I need to go through the steering mechanism to see what
is worn.
At some time I also have to address the fact that all the
electrics have been cut off short, so it needs a complete re-wire. I
have a full set of instruments, but no cables/pipes/drives to make them
work and no front lights. Aaaarghh.
My very good
friend Ian Johns, who passed away in 2019, used to take about ten years
per car and resurrected some real wrecks to good running order. Nothing
flustered him and he was always ready to make a cuppa and talk. I feel
him on my shoulder as a calming influence and guiding guru.
Got to get the painting done while the weather is good, and then get
into body building.
Pt 3 -
Winter, what winter? I only started work on the Austin in July 2019. I had removed the body and started working on the
chassis and renovating some of the parts that were salvageable with the
help of Andrew Jarmin and various service providers (clutch, gearbox,
torque tube, axles, suspension, dynamo and starter motor). My next task was to go from this
incomplete pile of bits to a rolling chassis.
Luckily I had a 1930 engine, complete with a nearly new Phoenix crank,
Supaloy high compression head and oversize valves. It was not
contemporary with the chassis or gearbox, but I thought it was a runner.
That was until we opened it up for inspection and found chunks of
aluminium lying on the gauze oil strainer. I collected all of these and
pieced them together like an archaeologist. They formed a neat ring that
puzzled me until I realised that they were the front bearing retaining
lip that is part of the rather delicate aluminium crankcase casting. I
was in deep despair as I assumed that meant a new engine.

Pieces found on the sump oil strainer.

New bearing lip bolted
inside the crankcase
.
Fortunately I also have the help and enthusiasm from Tim George who
lives nearby and I had not counted on the resourcefulness and skill
of the A7 fraternity. I found that Ruaridh Dunford at Alba Austins in Glasgow could fix
it by machining the lip flat, inserting a steel ring and bolting that to
the front bearing plate. I happened to be going to Scotland for some
mountaineering and arranged to meet Ruaridh at his garage. He not only repairs Austins but uses them for family
holidays.
Having fixed the bearing lip, we then had to give the engine a rebore to
20thou oversize (Paul Ince in Plymouth) and new pistons and rings -
taking care to gap the rings correctly (3-6thou). Andrew helped
me to install new valve guides and Tim’s engineering expertise was used
during the engine rebuild to ensure the flywheel runout and camshaft end
float were within limits. During the assembly of the conrods onto the
crank, we used Plastigauge to measure the journal clearances. These were
all between 1.5 and 2 thou, which is within the acceptable tolerance
range. The car came with its very non-standard 1 1/8” twin SU
carburettors in a very corroded state in a bucket full of builder’s
rubble. They were cleaned (airline, flapwheel + carb cleaner). Overhaul
kits were obtained from Burlen Ltd., and the carbs re-built, including
new float and main jet needles.

The twin SU carburettors after air
hosing out the dust and rubble.
Cleaned and working.
The
aftermarket Dante “bunch of bananas” exhaust manifold was mounted on the
block and the inlet tubes inserted with hand-made gaskets. These are
home-made castings and are a very tight fit. It proved very difficult to
do up the retaining brass manifold nuts, so all but the two outer studs
were removed and allen-headed machine screws
substituted.
A “mock-up” rolling chassis was assembled with engine,
carburettors, dynamo distributor, fan and pulleys, gearbox, prop shaft,
torque tube and handbrake mechanism loosely in place. This brought to
light a number of issues. The engine rocked on its mountings because the
driver’s side chassis member was bowed. The gearbox fouled the front
chassis cross member because the engine mountings on the older engines
are ¾” further forward than the later engines. The gearbox had a small
crack near one of the bellhouse mountings, and four out of six bolthole
threads for the gearbox cover were stripped.
The chassis member was
straightened using a stout 5ft steel girder and clamps. The engine was
moved forwards about 7/8” by drilling new mounting holes in the chassis. This had to be done very carefully so that no components subsequently
fouled one another. The engine was raised about 4mm at the rear and 2mm
at the front. The chassis had been boxed for rigidity, so where the rear
engine mounting bolts went through we provided a ¼” steel plate
underneath the chassis so that we didn’t distort it on tightening. The
gearbox cracks were drilled and the drill holes filled with silicone,
while the stripped threads were helicoiled.

Tool of all trades, Tim
straightening the chassis
This all allowed the engine and gearbox to be
solidly installed, complete with clutch, carbs, manifolds and starter
motor. The radiator (with a new “modern” core) and hoses were then
added. Initially there were leaks from the top water branch and the
bottom hose, but these were rectified.
At this point we decided
that we had
everything in place to start the engine. We connected a battery to the
starter motor, and wired up the distributor and coil. We also rigged a
petrol tube to the carburettors and had a fire extinguisher handy. The
next 3 hours we tried everything to get it to run. It seemed to fire and
then falter every time. It so nearly ran that we kept trying different
things, checking firing order, sparks at contact breaker and plugs, and
experimenting with more or less advance at the distributor. We
dismantled the twin SU carbs and re-built them, all to no avail. It was
all a bit reminiscent of when I first tried to start the car in 1967. Then, as a lad of 17 with no mechanical knowledge, I connected the HT
leads to the plugs in the logical order of 1, 2, 3, 4 and got my mates to
push me. They pushed and pushed and occasionally the engine would fire
and send the wheels backwards! Only when someone told us to connect the
leads 1, 3, 4, 2 did it go. We were waiting for a similar eureka moment
more than 50 years later, but none came. Had I learned nothing in those
50 years?
Eventually we realised that we had to go backwards to go
forwards. We removed the carbs and manifold, the starter motor and
gearbox – checking each in turn and dismissing them as the principal
source of the problem. At this point we noted that the flywheel was
really hard to rotate, and when we did so a squeak was heard. We removed
the engine and pulled off the flywheel. No obvious problem, so we took
the cylinder head off and all was revealed. Water had leaked across the
head and into the bores. This had caused surface corrosion and the
pistons were virtually stuck in their bores. WD40 and careful rocking of
the pistons freed everything up. The cylinder head was skimmed 6 thou by
West Cornwall Engine Services, and a new high compression gasket fitted. This time (7th February 2020) the engine fired readily and, after
adjusting the carburation, the motor ran sweetly.
This restoration has
been made all the more challenging by the “bitsa” nature of the beast, a
1930 engine with after-market head and manifold, 1933 chassis and
gearbox, 1920s starter motor and 1950s brakes and body. The Dante
manifold meant designing a bespoke exhaust system. A standard downpipe
was chopped up to provide the flange and 4” of pipe for a piece of 39mm
internal diameter stainless steel flexible exhaust pipe to connect, via
another 6” length of downpipe, to the standard exhaust pipe that is
mounted front and rear to the chassis with home-made clamps. We are
really pleased with this as it looks as if it comes off a Spitfire, and
works as intended.

Eat your heart out Lamborghini, that home-made
exhaust is peachy
With newly blasted and powder-coated wheels,
overhauled steering box, courtesy of Cornwall Austin Seven Club Teach-in
led by Andrew, and new Longstone 4.00/4.25 x 17 tyres we now have a
rolling chassis. The engine runs, the water circulates only where it is
meant to, and the transmission drives sweetly through the diff to the
rear wheels.
By any standards that is progress, but we are still in the
foothills. We can see problems getting the non-standard hydraulic brakes
to work well, and the racing fly-off handbrake needs actuating parts
making. We have no idea if the body tub will fit back on now that we
have changed the location of the engine and have a different starter
motor. In addition, we will have to make new body panels, floor and
seats. There are no electrics and most of the instruments need
attention. Ho hum, I guess that is what the summer is for.
Pt 4 -
Lockdown special In
February 2020 the rolling chassis had no brakes, no body, no electrics,
only a couple of functioning instruments and no seats. There was however
a body tub, constructed in the 1950s by Super Accessories from aluminium
sheet on an ash frame. Luckily, the wood frame had survived remarkably
well, so this was treated with preservative and the aluminium was
cleaned up as well as 70 years of dents and scuffs would allow.


Front
and rear views of the body tub before cleaning and “modification
”
Because the original 1933 engine had been stolen, and the replacement
engine was from around 1930, the gearbox, a four-speed from late 1933,
and the starter motor, a 1920s “bacon-slicer”, I wasn’t sure that the
body tub would now fit around this miscellany of parts. We offered it up
and sure enough had to cut out a space for the starter motor. We also
had to make a new throttle linkage on the inside of the bulkhead as the
original fouled the starter motor. All in all, the tub went on and came
off about four times before we got it right.
The braking system of the
special was based on Morris Minor hydraulics and a “fly-off” handbrake. The handbrake lever was fine, but the rest of the mechanism had to be
replaced. Tim made a new rod that passed through a gland in the rear
chassis cross member, and connected to the original equalising bar. New
Morris Minor handbrake cables were then shortened and connected to the
equaliser and thence to the rear slave cylinders. Fortunately I had the
four brake back plates, and we built these up with new Morris Minor
brake springs, brake shoes and slave cylinders. A set of Morris Minor
brake pipes, master cylinder and splitters were obtained, plumbed in,
and bled until it all worked. “Mecanic” silicone brake fluid, which
doesn’t attract water and doesn’t harm paintwork, was used to fill the
system. Sounds simple written down, but it took a lot of fettling
because we had to modify everything to fit, making sure we didn’t
compromise any other component of the car – in particular making sure
that the brake pipes did not chafe on anything or foul any of the
steering arms.
With the body tub on and the braking system installed we
could now turn our attention to the fuel system. We had previously
tested the engine complete with its twin SU carburettors using a
lashed-up tube to feed the float chambers. Now we installed the
carefully cleaned tank at the rear of the car, and threaded new ¼”
copper fuel pipe from the tank to a float-bowl filter and thence to a
new electric SU fuel pump.

Engine compartment starting to look more
complete. At this point we still needed a water temperature sensor in
the top hose and all the electrics including a cut out and fuse boxes.
The brake master cylinder can be seen on the far side of the engine.
What we should probably have done at this point was to install the new
electrics. In fairness to ourselves we did install the battery in a
compartment behind the driver’s seat, the positive lead to the starter
motor and the main earth to a bellhousing nut on the gearbox. We
deferred doing the rest of the electrics because: a) we didn’t have the
new cables and connectors at that time, and b) we were itching to get on
with the rear end of the car as we had no idea how that was going to go
together.
So, we mocked up the rear end with the various bits of wood
and aluminium sheet that came with the car and got the general idea. The
aluminium panels were torn and rough and needed to be replaced. While
some of the wood frame was serviceable, the whole back end was judged to
be too flimsy to carry the petrol tank, luggage and the spare wheel. We
therefore re-enforced it with extra bracing spars of ash, using dovetail
joints. A new 9mm marine ply floor was made for the rear luggage space
(this is pretty small, having about 75litres capacity – the same as a
large rucksack).
T
his might look brutal, but in Tim’s hands a mallet
is a precise weapon.

The back end takes shape and gains strength.
As the
body tub, the cockpit floor, the bonnet sides and the rear end woodwork
are fixed securely in place suddenly everything is much taughter. The
car is still light and somewhat vulnerable to being T-boned by a milk
tanker, but it now feels agile and of a whole.
Much debate was had about
the colour scheme. Should we leave the body bare aluminium? What colour
should the cycle mudguards be? Eventually I decided that the aluminium
should stay, proudly displaying its rough and tumble history. The
mudguards have been prepared in primer and gone to a local car sprayer,Tim Poore at Tregony, for topcoats in Lotus Yellow. This is near to the
colour when I had the car 50 years ago, so feeds my nostalgia itch
perfectly. Also everybody knows that Lotus evolved from Austin 750
racing, so there is a direct and legitimate connection.
Lockdown has
meant that I have had more time to work on the car, and suppliers such
as The Austin Seven Workshop, Paul Beck and Holden Vintage and Classic,
as well as on-line tool and fastener suppliers have been brilliant at
sending bits and pieces. Often it has taken a lot of detective work to
sort out the precise part for the job as we attempt to create something
unique, but so far so good.
The proof of the pudding will be how it
performs on the road. With a low-power engine, primitive suspension and
design by intuition we don’t expect sparkling performance. The first few
outings will be very local, with a following car to pick up the bits
that fall off, a full tool kit and a tow rope. Hopefully that will be
before the end of the summer. A two-page list of outstanding tasks
confronts us, so better get out of the kitchen and back into the
workshop.
Pt 5 - ShakedownA major difficulty has been the mongrel nature of the beast,
comprising a 1933 chassis and gearbox, a 1930 engine, a 1950s body and
braking system and a 1920s starter motor. This has required us to make
some parts from scratch and to compromise on originality.
We
have learned that the way it was put together as a Special in the 1950s
was not necessarily the best way, and we have learned the value of
advice and support from Andrew. While the car is mine and I am responsible for all mistakes made
along the way, I have been heavily dependent during the re-build on my
friend Tim who has a deep empathy and skills for all things metal and
wood. Together we three have re-built the engine, gearbox, carburettors,
exhaust system, steering, entire braking system, rear-end bodywork,
suspension, seating and electrics.
Working on the rear end of the car
the new woodwork which had been fitted was stronger than the original, and now we set about replacing the old,
bent, ripped and corroded panels with new ones made from 1.2mm aluminium
sheet. We cut this with a jigsaw using the old panels as a rough
template. We then bent them, bonded and screwed them in place, and
perfected the fit using a rasp and various files. The shiny aluminium
was then sanded to provide a finish that was consistent with the old
panels on the front of the car. Half-round aluminium strip was used to
cover seams where two panels butted together. Given that neither Tim nor
I had done anything like this before we were very pleased with the
result.



The original car had the spare wheel mounted on the back end
supported by brackets, and a sort of trailer bar on top of that for the
number plate and rear lights. We decided that was too messy, so
opted
to mount the spare wheel on an old brake drum. We obtained a drum and
two wheel-stud carriers from Andrew. We welded the carriers back to back
and fixed it all solidly to the rear end. The wheel sits flush with the
bodywork and looks good. The rear lights, stop/tail, indicators,
reflectors and number-plate illumination, were all installed on the rear
mudguards and look neat and tidy there.
Some of the mudguard fixing
brackets were missing, so we got Tony Pascoe Engineering at Par to make
up some new ones. After ages spent fettling, we got these to fit, and
also fitted the head/side lights, rear stop/tail lights and front
flashers. Some instruments were missing or broken, so we obtained a new
ignition switch, ammeter, temperature gauge and on-on dip switch. A
temperature sensor was plumbed into the top hose; it sounds simple, but it
took a bit of sleuthing to find the correct sized adaptors.

Having
fitted the lights, our next job was electrics . When the previous owner
had started to strip the car some 20 years ago he had simply cut all
cables to the lights, instruments and controls - meaning we had to start
from scratch. We obtained a second-hand cut-out and bought a new
period-looking fuse box. Because this is not a standard model we decided
not to buy a ready-made loom, but to purchase the individual cables. We
went for plastic-coated, thin-wall cables from Auto Electrical Supplies,
keeping where possible to the correct colours and choosing the cable
cross sectional area according to the peak current that it would be
carrying. We earthed everything back to the engine block and fused all
lights and instruments. A master switch was added on the battery post,
and an in-line 30amp fuse installed on the cable to the starter switch.
Flashng indicators have been added for safety, so a flasher relay is included.
The top photo above includes the gearbox, and a stubby lever emerging
from it. Originally this was operated by a rod to a remote gear lever
further back in the car. However, this had a poor mechanical advantage
and it was hard to change gear. We therefore obtained a second-hand
lever from Andrew to operate the gearbox directly, and bent it with
lots of heat to a suitable profile. We had to make a new locating pin
as the old one was seized in place, and bought a new knob from The
Austin Seven Workshop.
All the main mechanical and electrical elements were
now in place. The last time the engine was started we used the bare
chassis as a test bed. Since then the body, floor, fuel tank, rear body
panels, mudguards and electrics have been fitted. Now we itched to try
out all of those components. Temporary seating was rigged up and the
engine started. After warming the engine through it continued “hunting”
so the twin-SU carburettor adjustment nuts were wound in to make the
mixture leaner.

On the farm track it was quickly apparent that although
the engine and transmission were working well, the steering was heavy
and the brakes poor. The drag link was detached to see if the steering
resistance was in the linkages or in the steering box. The box, which
had been overhauled, seemed to have the right amount of resistance, and
we felt the main source of heavy steering was in the king pins. The king
pin caps were not seated well and so grease was not reaching the main
swivel areas of the king pins. We did not want to dismantle the whole
front end to re-tap the cap threads at this point, so have made do for
the moment with lubricating things as well as possible. We are finding
that with use, the steering is freeing up. However long-term the king
pins need to be properly greased, so the front axles will get a thorough
strip down over the winter. We also adjusted the toe in by reducing the
length of the track rod, and improved the castor angle by twisting the
radius rods.
The hydraulic brakes were disappointing, so Tim and I
decided to run up and down the track quite a few times using the brakes
as much as possible to bed the new shoes in.
After a while they
started to bite more convincingly, so we were encouraged to re-adjust
the front and rear brakes. The front brakes adjusted up quite a bit, and
we found that there was a weep of brake fluid at the nearside rear
brake, rectified by nipping up the banjo bolt.
The brakes were re-bled
and now the car stops quickly and in a straight line. Everything else
seemed to function properly. The thermosiphon cooling system works well,
the oil pressure stabilises around 7psi when the oil is hot, all the
electrics and instruments work except that the dynamo output is a bit
low at around 4 amps.

No seats came with the car. When I owned it in the
late 1960s I just used cushions that used to slide around dangerously.
With an MOT looming we decided to improve that situation by making seat
bases that were locked in front, back and sideways. The seat back has to
allow access to the “luggage compartment” behind the seat. This was a
design nightmare. We tried and rejected a hinged arrangement, and
eventually opted for a lift-out unit that locks in place as it is
inserted. Upholstery of the bases and back was undertaken by David Nudd
at Penzance using maroon expanded vinyl that matches the facia. The exact
same material and colour are still available from Woolies Trim Supplies
some 70 years after the original was acquired. Note the grommet in the
middle of the transmission tunnel that allows access for greasing.

While
the original special had a conventional windscreen, I happened to have a
pair of aero-screens in a cupboard and decided that these looked in
keeping with the low-slung Super Accessories bodywork. Tim made a wooden
plinth for the aero-screens and a rear-view mirror to screw into. This
leaves the car open to the elements, so I carry an umbrella in case of
downpours. The glove box shown here contains some items that had been
left in the car since the ‘60s, including Green Shield stamps and
pre-decimal coinage.
Now it was time for an independent assessment of
our work. Tim used a friendly MOT tester for his Land Rover
and old-style camper van, so we thought he would be an empathetic
appraiser. I drove the 20 miles to the testing station listening for any
sign of trouble, but miraculously got there in good order. I was greeted
effusively and asked to put “the beauty” on the ramp. Unfortunately the
car was too narrow, so he could not do the test. I then contacted another
tester and a fortnight later we passed with flying colours.
The last
piece in the jigsaw was to get the V5C taxation classification changed
from “Not Licensed” to “Historic Vehicle”. I took MOT, Insurance and the
V5C to Truro Post Office and after a bit of tapping on his screen, the
nice man proclaimed it to be accomplished (he had to post the V5C to the
DVLA who will eventually send me an updated version).

The re-build has
taken 22 months and a lot of enjoyable toil. I should come clean about costs. Excluding labour,
but including the very low purchase cost, total expenditure was
£11,840.65. The outlay is probably similar to the re-sale value of the
car, but that is academic as I won’t be selling it. Too much skin in the
game!

Apart from summer jaunts around the Roseland, my wife and I
eagerly anticipate packing the small luggage compartment with a few
essentials and crossing to France where the roads are quieter, the
locals appreciate small, quirky vehicles and the weather is a little
better. The number plate says it all: “Allez Ma Cherie”.
Lastly I must express my thanks to both Andrew Jarmin and Tim George whose
combined knowledge and skills have been shamelessly
exploited, but I think the end has justified the means. Andrew has
many years experience of working on Austin Sevens. Tim is a
boat-builder and mechanic living in Veryan on the Roseland. He
brought another level of expertise to the table, enabling us to make
items on the lathe, to sculpt and strengthen the woodwork, to make new
aluminium body panels and to carry out complex and delicate mechanical
operations on the engine, braking system, transmission and electrics.
These articles were written by Barry Pound
and appeared in Seven Focus. Pt 1 in March 2019 pp 9-11; Pt 2 in September 2019 pp 7-10;
Pt 3 in March/April 20202 pp 11-16; Pt 4 in July 2020 pp 13-17 and Pt 5
in November 2020 pp 3-9.
Appendices:
1.
Renovation action by car component
Chassis: Number
179566. First registered on 27 October 1933. Long wheel-base (6ft
9ins). Has had front centre chassis member on which cable brakes pivoted
replaced by aluminium tray.
Condition at start of renovation: Good. No significant corrosion,
cracks or loose rivets. Rhs main side chassis member was bent down about
8mm from straight.
Action taken: Cleaned up by hand and painted with 2 coats of
Hammerite Red Oxide and 2 coats Frosts extreme chassis black.
Straightened rhs chassis member by clamping it up to a steel girder.
Front mudguard stay “outriggers” made by Tony Pascoe engineering (Par)
and fitted to chassis.
Comment: Body off in July 2019. First road test (with no seats or
aeroscreens) August 2020. Brakes and steering still in need of fettling.
Body: “Super Accessories” Super model. Made in the late 1950s
with 20-gauge aluminium on ash – see
http://www.oldclassiccar.co.uk/superaccessories.htm
Condition at start of renovation: Aluminium body parts
(bonnet, engine side panels, main body tub) that could be saved were
straightened, cleaned, sanded and polished.
Action taken: The body tub was offered up on March 21 2020. A
number of adjustments were needed because of changes made to other
components. A hole had to be cut in the bulkhead to accommodate the rear
facing starter motor. A body-stiffening crossmember had to be re-located
due to the handbrake cables having been re-routed. The throttle rod
mechanism had to be altered due to the new location of the starter
motor. Tim made new cockpit floor from 9mm ply. This was surfaced with
1.2mm aluminium bonded with epoxy and painted with marine quality
primer. The underside (ply side) was coated with underseal. The rear end
aluminium body panels were in poor condition, but acted as templates for
new panels.
The woodwork was replaced with new ash by Tim to provide a useable
storage space at the rear, and sufficient strength to hang the spare
wheel on the rear end. Tim added extra bracing and shaping spars to the
rear end. The floor of the rear storage area was made from 9mm marine
ply. New rear panel blanks were cut from 1.2mm aluminium sheet in early
May 2020 using the old panels as templates. The back-end roundel panel
was bonded to its plywood base with marine epoxy adhesive and then cut
and shaved precisely to shape and also screwed with ½” x 2g brass
screws. Then the two rear wraparound pieces were offered up, bent to
shape, marked, trimmed and fitted using small screws and adhesive.
Aluminium half-round beading was used to hide butted seams.
Spare wheel mounted on rear end of car using a brake drum and two
wheel-carriers welded back to back and bolted to the rear end.
Made new torque-tube tunnel from 2mm aluminium sheet. Incorporated holes
with rubber grommets so that the torque tube and front UJ can be greased
regularly. Self-adhesive number plates applied to rear bodywork.
Comment: Body off in July 2019 and back on in March 2020.
Interior:
Condition at start of renovation: Fair to good.
Action taken: New
floor in 9mm marine ply with aluminium skin. Fitted vinyl loop to glove
compartment door. Woolies Trim maroon expanded vinyl is the exact
material used for the upholstery (have 1m for repairs).
Seats:
Condition at start of renovation: No seat frames or
seats.
Action taken: Seats were made from scratch (seat frames and
cushions and a seat back that lifts out to allow access to storage
compartment made by Tim). High impact foam and maroon expanded
vinyl obtained from Woolies. David Nudd did the upholstery.
Comment: Started 25 July 2020
Bonnet:
Condition at start of renovation: Fair.
Action taken: Dents hammered out. Fitted over-centre catches.
Obtained and fitted leather strap and buckles (from Paul Beck).
Engine: Number
M138287 (15/16” crank). Believed 1930. Coil ignition. Supaloy head;
Phoenix non-pressurised crank. Cylinders had been sleeved to standard
bore, but rings were worn. Oversize valves. Re-built by Vince Leek in
1990s.
Condition at start of renovation: Good.
Action taken: Obtained parts (fan assembly, valve chest studs
and knobs, Water inlet, dipstick, oil filler tube and cap, oil pressure
union, starter motor). Cleaned externally; de-coked and ground in
valves. Dropped sump and found crankcase front bearing retaining lip
broken. Repaired retaining lip (Ruairidh Dunford, Alba Austins,
Glasgow). Studs for water inlet bent and cracked seating. Straightened
studs and modified water inlet. Replaced broken manifold studs Renewed
valve guides. Lapped in valves again. Obtained new 4-ring JP
pistons/rings and re-bored to +20thou (Paul Inch Engine Services).
Rebuilt engine at the elbow of Tim George. No 4 big end tight so scraped
white metal until free. Used existing bearings. New gaskets. New oil
pump springs and ball valve. New rear crankcase seal. Flywheel runout
and camshaft end float within tolerances. NB Tim tapped new threads into
flywheel for puller. New tab washers all round. Painted block with
Frost’s engine enamel. Filled engine with Penrite Classic Light 20W-50.
Recommendation after initial running in is Penrite Shesley Light 20W-60.
The early engine had engine mounting holes ¾” further forward than later
engines. This meant that when coupled to the 4-speed gearbox the
combination was too long and the layshaft cover bolt fouled the front
chassis cross member. We drilled new engine mounting holes in the
chassis 7/8” forward of the originals. This meant other items were a bit
tight, but with a bit of fiddling everything was made to fit. 100mm x
M10 engine mounting bolts used at the back. ¼” steel plates under the
chassis to stop the mounting bolts collapsing the boxed section.
On attempting to start the engine there was leakage of coolant across
the head gasket into the top of the bores. The head was removed and
skimmed by West Cornwall Engine Services (taking 6thou off). Engine
first started 7 Feb 2020 using the chassis as a test bed!
First road test with all components in the car in September 2020.
Misfire due to sticking valve. Cured with lubrication and tapping valve
head with light hammer. Ran for 30 mins on idle. No problem after.
Comment: Engine fully disassembled end Aug 2019. Crankcase
taken to Glasgow early Sept. Re-bore done Oct 2019. Head skimmed Feb
2020. Engine started Feb 7, 2020
Gearbox: 4-speed with synchro on second and third. Correct for
late 1933.
Condition at start of renovation: Good.
Action taken: Penrite Classic Light 20/50 oil used. The
gearbox casing cracks were drilled and then filled with silicon. 4 cover
bolt holes were helicoiled. One helicoil tab not accounted for.
Magnetic insert glued into drain plug in attempt to catch a helicoil tab
that might have entered the gearbox. Remote gear lever rod broke at weld
on gear stick. A second-hand gear lever was obtained from Andrew
Jarmin, and bent downwards and sideways to the right using a propane gas
gun to heat the shaft to a glowing red. A new location pin was made from
a ¼” bolt and a new gear knob obtained from The Austin Seven Workshop. The
new lever has far better mechanical advantage than the remote linkage,
so finds gear easier and smoother.
Comment: Overhauled with Andrew Jarmin on 29 July fitting new
bearings, balls and springs.
Clutch:
Condition at start of renovation: Good.
Action taken: Good lining on flywheel. Parts sourced through
Andrew Jarmin and Holmesdale Sevens (Tony Leslie). New starter ring
machined/shrunk on by Paul Bonewell. Installed clutch (after false start
thinking we had 3-speed toggles).
Prop shaft: Sports
propshaft with Hardy-Spicer joints at each end. UJs seem OK.
Condition at start of renovation: Good.
Action taken: Changed orientation of UJs so joints line up.
Cleaned and painted shaft. Turned front end of shaft in lathe so it
fitted the output drive from the gearbox
Torque tube: Changed
torque tube, as it was cracked, for one supplied and fitted by Andrew Jarmin
Condition at start of renovation: Good.
Action taken: Cleaned and painted. Installed on original 4
holes in rear chassis cross member (much lower than before). Now
articulates well. Checked mesh with diff.
Front axle: Lowered.
Condition at start of renovation: Good. Partially dismantled.
Action taken: Cut track rod threads with 3/4x20 die. Reduced
length of track rod by about ¼” at both ends and adjusted to around zero
toe in. King pins are good. Found that front axle was bent and twisted.
Sent standard axle from Andrew Jarmin for modification to sports spec.
(and eyes shrinking) by Ruaridh Dunford, Glasgow.
Front spring: Flattened.
Condition at start of renovation: Good.
Action taken: New grease nipples to shackles
Front shock absorbers
Condition at start of renovation: Poor.
Action taken: Unserviceable so bought new sports double
friction damper suspension unit.
Front radius arms:
Lowered
Condition at start of renovation: Fair.
Action taken: Replaced left hand radius arm. Also replaced cups
and spring at rear end of radius arms. Replaced the radius arm ends and
shackles with sports radius arms from A7Components
Rear axle: D-type (two
piece)
Condition at start of renovation: Good.
Action taken: Filled with 7/8 pint of Penrite Transoil 140
Rear springs:
Flattened.
Condition at start of renovation: Good.
Action taken: Replaced U-bolts as one cracked through.
Rear shock absorbers:
Standard
Condition at start of renovation: Fair.
Action taken: replaced with new.
Starter motor: Was
missing
Action taken: Fitted CAV Bacon slicer starter motor and
integral foot operated switch supplied by Andrew Jarmin. Cleaned
commutator and checked bushes. Machined carefully to fit.
Carburettors: Twin 11/8”
SU carbs (H1-type)
Condition at start of renovation: Corroded and filthy.
Action taken: Cleaned up and replaced internals with new
gaskets, new float needles, main jet needles and other new parts. Check
float level -
http://sucarb.co.uk/technical-h-type-carburetter-diagram article.
Custom made copper tube mixture balance pipes (Tim).
Battery: Negative earth;
6Volt. Type 421
Action taken: Purchased from Holden Classic. Filled with acid
and charged (Jan 2020). The battery was earthed on a gearbox bellhousing
nut so that there was good connection through to the starter motor.
Master switch installed on battery post and in-line 30-amp fuse fitted
to the feed to the starter motor.
Dynamo: Lucas Y 220299
6V. Tested by Andrew Jarmin and works. Third brush adjusted to 10amps. Negative Earth.
Action taken: Installed with distributor and fan assembly.
Distributor: Type BN24; Model DK4A.
Condition at start of renovation: Poor.
Action taken: Very corroded inside. Had to free everything up
(spindle, weights). Sent to Distributor Doctor for rebuild (Martin Jay).
Now beautiful. Installed and wired up HT leads to new plugs and new
coil (soldered all ends).
Coil: Was Wipac 6v Type
S2730.
Condition at start of renovation: Poor, this was punctured and
oil leaking out.
Action taken: Replaced with new coil.
Cut out and fuse box:
Separate units
Condition at start of renovation: Good.
Action taken: Purchased from 7 County Austins (Tony Betts).
Additional 8-fuse fuse box installed.
Wiring loom:
Condition at start of renovation: Mess, a bag of wires cut
from instruments and lights. .
Action taken: Thin wall cable in Austin 7 colours purchased
from AES together with a box of connectors, spiral binding and heat
shrink. Decided against buying a ready-made wiring loom. Purchased
8-fuse fuse box and 4-way junction box. Wiring started in late June with
the rear lights and rear indicators. Cables were bundled in spiral wrap
and routed up the torque-tube/prop-shaft tunnel to the bulkhead.
Instruments: Speedometer;
Tachometer (mechanical); clock (works); water temperature; fuel gauge
Condition at start of renovation: Dials OK, but tubes/cables
missing.
Action taken: Purchased and fit new speedo drive. Oil pressure
gauge appears to work fine. Fitted with new copper pipe and fittings. Purchased new water temp gauge (from A7 Workshop) and sensor, and
T-piece sensor housing (from Holden Vintage and Classic). Rev counter
take-off machined to take drive from underside of distributor spindle.
0-8 amps Ammeter gauge purchased from Holden Vintage and Classic, but
charge and discharge was more than this, so bought 0-30 amps ammeter off
e-Bay. Fit all gauges and switches to dashboard, discarding the central
console that was used originally. Renewed some switches, including new
Lucas ignition switch and on-on dip switch.
Lights:
Condition at start of renovation: Head/side lights
missing. Tail lamps OK. Indicators missing. All 6volt.
Action taken: Purchased 5.75” headlamps/sidelights, plus
mudguard-mounted front flashers and mudguard-mounted rear flashers,
stop/tail lights and reflectors (Paul Becks). Inserted clear glass
window in stop lights to provide illumination to number plates.
Installed interior light in luggage space and a dash light for map
reading.
Steering:
Condition at start of renovation: Good.
Action taken: Lhs radius rod very pitted and replaced, together
with spring and cups Put in new drag link springs and cups and ball
joints. Overhauled track rod ends with new pins, bushes and cotters
Overhauled and greased steering box (Andrew Jarmin masterclass 16 Nov) –
rotated column setting through 180deg, and moved box gear through 120
deg to less worn segment). Adjusted play. Horn wired through steering
column
Brakes: Were Lockheed
hydraulics (7” Morris Minor). Most parts apart from back plates and rear
drums missing.
Condition at start of renovation: Poor
Action taken: Purchased master cylinder, slaves, drums, pipes,
splitters etc. from Charles Ware. 2 drums with car, 2 purchased from
Ruairidh Durnford (Alba Austins). Custom made bracket for mounting
master cylinder (Tim). Front brakes went together easily, but rear
brakes required trial and error. First mounted rear slaves with
handbrake lever upwards. Decided this meant it would be difficult to
bleed brakes so dismantled hubs and reversed the slaves. Then brake
shoes didn’t both expand when brake put on so dismantled hubs again (!)
and swapped backplates round. Then all seems to work properly. Brakes
filled with Mecanic silicone brake fluid. Bedded in on shakedown and
then re-adjusted up. Now work well.
Handbrake: Sports fly-off
Condition at start of renovation: Good
Action taken: Removed and cleaned. Custom-made (Tim) rod, and
equaliser with new bracket. New handbrake cables obtained from Charles
Ware. Shortened to fit and cables joined using drilled brass rods and
solder.
Exhaust System: Dante
manifold OK, but silencer and tail pipes absent.
Action taken: Purchased some parts from Holmesdale Sevens
(downpipe from which to make manifold to pipe flange, silencer, clamps). Also a length of 39mm ID stainless flexible exhaust pipe from Whitehouse
Flexible Tubing Ltd. From these fashioned a bespoke exhaust system.
Fuel supply:
Condition at start of renovation: Good.
Action taken: Fuel tank cleaned out and painted. Replacement
neck and fuel filler cap from Paul Beck fitted. Replaced ¼” copper fuel
lines to include in-line fuel filter/sight bowl. Replaced fuel pump
with new electric SU pump (Type AUA 26).
Radiator:
Condition at start of renovation: Good.
Action taken: New core obtained from Hereford Radiators. Fan
blade is rather close to the top radiator hose. Need to keep an eye on
this. Fixed leaks from top water outlet by use of cork gasket and blue
Hylomar. Purchased wiggly hose from Car Builder Solutions. Temperature
sensor fitted to top hose.
Wheels, tyres and hubs:
Were 17”. Front tyres 4.00x17; Rear tyres 4.50x17. Changed to
17x4.00/4.25 all round.
Condition at start of renovation: Good.
Action taken: Sand blasted and powder coated by Blast and Clean
(Longdowns). Purchased 5 tyres, tubes and rim tapes (all 17x4.00/4.25
Longstones). Replaced bearings, greased hubs. Replaced wheel centres.
Spare wheel mounted on rear end of car using a brake drum and two
carriers bolted to the rear end.
Steering wheel:
Condition at start of renovation: Fair.
Action taken: Repaired flaking plastic with fibreglass and then
painted with Matt Black spray paint. Not effective so bought steering
wheel overhaul kit from Paul Beck. Stripped s/w to bare metal. Repaired
dents with supplied epoxy and then painted with 2-pack acrylic epoxy
paint supplied with kit. Sufficient materials for at least one other
steering wheel.
Hood:
Condition at start of renovation: Good.
Action taken: Frame seems all there. Hood cleaned. Small cracks
in Perspex, but serviceable. Hood irons cleaned, sanded and painted.
Comment: Hood not fitted as does not work with aero-screens.
Mudguards (Wings):
Condition at start of renovation: Good.
Action taken: Blasted and primed (together with brackets) by
Blast and Clean (Longdowns). Dents then filled and mudguards re-primed.
Tony Pascoe Engineering (Par) made brackets and chassis outriggers for
front mudguards. Painted (Tim Poore) Lotus Yellow (L07). After
completing installation and electrics, painted inside of mudguards with
Hammerite Waxoyl Underseal. Fitted mudflaps to front mudguards.
Windscreen:
Condition at start of renovation: Poor.
Action taken: The windscreen glass was smashed by shed
collapse, and the surround mangled. Straightened surround, but fit is
still poor. Decided to fit Aero-screens instead (look better). Means we
can do away with windscreen wipers and washers, but also means we can’t
fit the hood. Tim made wood “plinth” on which to mount the
aero-screens.
Miscellaneous:
Chassis painted (2 coats Hammerite red oxide + 2 coats Frosts
black extreme chassis paint)
Block painted with Frosts Engine enamel.
Electrical components primed and spray painted with Hammerite Smooth
Black;
Mudguard sprays painted with Simoniz tough black spray.
Preservative and varnish for woodwork.
Fuel additive (Castrol Valvemaster), Mecanic silicone brake fluid.
Penrite Oils (Shesley Light for engine and gearbox, Transoil 140 for
diff.)
Duralac, Hylomar Blue, 3M marine adhesive.
Tools (heat gun, rivet gun, step drill bit, countersink drill bits, hub
puller, flap wheels and wire brush wheels, metal shaping hammers and
dollies, jig saw and blades, pillar drill, crimping tool and copper pipe
flaring tool with pipe cutter).
Nuts, bolts, screws, washers – mix of Whitworth, BSF and metric. 9mm
marine ply, ash for spars, iroko for seat back rest, spruce for extra
timber components, 1.2mm and 2mm aluminium sheet for floor, body and
transmission tunnel, ½”, ¾” and 1” half round aluminium strip for
covering joins between panels.
MOT (October 2020). Registered as Historic Vehicle with DVLA.
2. Renovation
services/sources
Cornwall Austin Seven Club:
http://www.austin7.org
Technical help and parts from Andrew Jarmin..
Austin Seven Workshop,1A Cornish Way, North Walsham, Norfolk NR28 0AW.
Jamie Rogerson.
https://www.theaustinsevenworkshop.com/ ;
info@theaustinsevenworkshop.com ; Tel: 01692 407507.
Hereford Radiators, Berrington St, Hereford, HR4 0BS. Tel: 01432 274227;
sales@herefordradiators.co.uk
http://herefordradiators.com/home.html
ERS (RH) specialist motor insurance:
https://www.ers.com/ ;
rh@ers.com
Tony Pascoe Engineering Limited,
https://www.tonypascoeengineering.co.uk/ ;
tonypascoeengineering@hotmail.com Unit 17, St Austell Bay Business
Park, St Austell, Cornwall PL25 3RF. Opposite Par Market. Tel: 01726
813817. Fabrication of metal parts.
Keys cut to code on e-bay (Ignition key):
https://www.ebay.co.uk/usr/keyscuttocode
Mercury Vintage Services: Austin Seven Manual.
Susan.woodrow@gmail.com ,
Mercury Vintage Services, Rosedale, Station Road, Emneth, PE14 8DL.
Tel: 01945 430058
A7 Components: David Cochrane. 18 Russell Avenue, Dunchurch, Rugby,
Warwicks CV22 6PX. Tel: 01788 522033. Website:
www.a7c.co.uk e-mail:
sales@a7c.co.uk Specialist in
Austin Seven parts
Seven County Austins:(Tony Betts): 0116 2867522: 31, Forest Road,
Huncote, Leicestershire LE9 3BH; Tel: 01162 867522;
tony.7ca@aol.co.uk ;
http://www.7ca.co.uk
Large stocks of new and secondhand spares
Woolies
(I & C Woolstenholmes Ltd): Whitley Way, Northfields Ind Est,
Market Deeping, Peterborough PE68AR. Tel: 01778 347347;
info@woolies-trim.co.uk
Drevo/Denso tape for wrapping springs
Holden Classic and Vintage: Linton Trading Est, Bromyard, Herts HR7 4QT.
Tel: 01885 488488
sales@holden.co.uk
Battery, catches etc.
ABS Metals (Easy Metals): Unit 4, Tregoniggie Ind Est., TR11 4SN
Falmouth; Tel: 01326 333494/378811;
www.absmetals.co.uk and
www.easymetals.co.uk . Aluminium sheet (1.2mm and 2mm) and flat
strap.
Holmesdale Sevens (Tony Leslie): Ashlee, Thetford Road, Coney Weston,
Bury St. Edmunds, Suffolk IP31 1DN; Tel: 01359 221838 (9am – 5.00pm);
holmesdale7@gmail.com
Mobile: 0786093731
Paul Bonewell, 52 Upper Close, Forest Row, Sussex RH18 5DX; Tel: 01342
822072. Machinist, starter ring, camshafts.
Distributor Doctor (Martin Jay): Tel: 01984 629540; Distributor Doctor
Ltd, Unit 8 Old Brewery Road, Wiveliscombe, Taunton, Somerset, TA4 2PW.
http://www.distributordoctor.com/distributor_advance_springs.html
Burlen Ltd (SU Carbs): Burlen Ltd, Spitfire House, Castle Road,
Salisbury, Wiltshire SP1 3SB.
info@burlen.co.uk Tel: 01722 412 500. Spares and renovation kits
for most carburettors.
Alba Austins (Ruairidh Dunford): 64 Campsie Drive, Bearsden, Glasgow G61
3HX. 0141 942 8037; Tel: 07754 171005.
Dunford1@aol.com . Crankcase repair
Charles Ware's Morris Minor Centre: 20 Clothier Road, Brislington,
Bristol BS4 5PS.
info@morrisminor.org.uk Tel: 0117 3003 754 (spares: John Knowles).
Brake parts
Paul Inch Engine Services Ltd, Unit 1, St John’s Road, Cattedown,
Plymouth, PL4 0PA. Tel: 01752 255563. Re-bore.
Blast Clean and Coatings, Lower Trolvis Works, Longdowns, Penryn TR10
9DL;
info@blastcleanandcoatings.co.uk ; Tel: 01209 861456
Paul Beck Vintage Supplies Ltd: Unit 7 Merebrook Business Park, Hanley
Road, Malvern, Worcestershire, WR13 6NP; Tel: 01684 212882;
info@vintagesupplies.com .
Lights; head, side and indicators.
Car Builder Solutions, Redlands, Lindridge Lane, Staplehurst, Kent, TN12
0JJ. Tel: 01580 891309 / 01580 448007 / 01580 448017 Email:
info@carbuildersolutions.com
.
https://www.carbuilder.com/uk
Hoses, fuses, radiator grille etc
Fuel system parts:
https://www.classic-spares.com/fuel-en/
Brass screws: Ossett Emporium, 7 Nettleton St, Ossett, W. Yorks, WF5
8HQ.
www.ossettemporium.co.uk
;
sales@ossettemporium.co.uk
Copper pipe and fittings:
https://www.vintagecarparts.co.uk/categories/vintage-car-parts-taps-pipe-and-fittings
Whitehouse Flexible Tubing, Britten Street, Redditch, Worcestershire B97
6HD. Tel: 01527 64036 & 62398; E-Mail:
sales@flexible-tubing.com
Flexible exhaust pipe
West Cornwall Engine Services: Unit 4A, Nancegollan Inds Est.,
Nancegollan, Helston, Helston TR13 0AP; Tel: 01209 831789. Cylinder
head skimming
SJ Andrew and Sons, South Turnpike, Redruth TR15 2LZ, Tel: 01209 213171;
http://www.sjandrew.com . Steel
and metalwork supplies.
Tim Poore, Autobody repairs: Pendarves Farm, Reskivers, Tregony, Truro
TR2 5TE; Tel: 01872 530584. Painted mudguards
David Nudd, rear of Marine Terrace, Penzance TR18 4DL. Tel: 01736
369419. Upholstery.