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15 April 2008 |
Little End Bolt Failure; Second ThoughtsIt is interesting to note that when our Ruby shed a little end bolt ( the day that we sold her to David ! ) she suffered two bent conrods as a result. This was exactly replicated by Mike’s engine when his failure occurred. On both engines one bolt failed and two rods were bent.
Recently I asked Mike about the condition of the little end bolt which failed in his engine. Again the bolt showed signs of fretting and there was a small length of the threaded bolt left in the con-rod. In the 12 months or so since our Ruby had the upset with the bolt Andrew Jarmin and I have periodically discussed the cause without coming to any definitive conclusion. However, the points that we have considered are thus;-
Having recently stripped down my spare engine which has done approximately 1500 miles I found two of the little end bolts showed signs of fretting. The engine had been assembled with new pistons and gudgeon pins so one should be able to discount wear in the gudgeon pin where it passes through the little end. The pins were a snug fit in the pistons but capable of being pressed out, cold, by hand. This appears to indicate that the pins had not seized in the pistons. Indeed the pins and pistons were in excellent condition.
The Pistons and gudgeon pins have been used, along with the block, to rebuild the engine in our Box Saloon. When I stripped down the existing engine, which had been sleeved to standard but was showing signs of considerable wear, there was no sign of any fretting on any of the little end bolts. When I combined the Box engine's con-rods to my spare engine's pistons and little ends I found that the gudgeon pin had to be pressed into the little end rather than just pushed in by hand. Upon reflection, perhaps this is how it should be! Is this the answer to the problem? Am I, are we, assembling engines where there is too much play between the con-rod and gudgeon pin in that the little end bolt cannot tighten sufficiently to prevent movement? When I reassembled the engine I made sure that I clamped the gudgeon pin, using jigs, in the vice whilst I tightened the little end and then made sure that there was no discernable movement. Hopefully this will ensure that the little ends remain intact. I must admit I have never used this method before and therefore never really checked how tight my little ends were. So I think the conclusions are, not only ensure that you use new bolts and locking washers ( or tabs ) every time but also check that the gudgeon pin is a tight fit in the con-rod and that the assembled piston does not allow movement between the gudgeon pin and con rod. Any comments? Malcolm Watts mwatts@uku.co.uk
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